Well a bunch of stuff I ordered from island 4x4 weeks ago finally came today so fitted new pollen filters and used some self adhesive draft excluders to seal them on the covers.
Redid the ptfe on the hose Barb for the reducer Barb I replaced last month as there was still a slight leak but no where near as bad as before.
While I was picking up the draft excluder from screwfix I checked to see if they did the gas leak spray and they did for £3 so picked up a bottle of that and sure enough no leak there now but could still get a faint whiff of gas so sprayed all the point and found it was on the T for the copper lines to one of the reducers so nipped that up and it stopped bubbling.
Replaced the overflow/return pipe as that would let a little coolant out of touch slightly so I didn’t think it was sealing too well, upon taking the old one of it literally snapped in my hands which explains why there was a bit of hose clamped on the over the corner of it I assumed maybe for protection to stop the corner from rubbing but nope it seems like someone did that to deal with a break before. There was no blockage in the previous one but did find the new one gave a much better stream into the tank where it was more of a dribble before.
Fitted a new genuine coolant cap as one the o rings on the other one were seeming a bit flat but would also sometimes getting hissing after stopping from it unless really cranked down. the system was still under pressure so it wasn’t actually letting any coolant out but still.
I did find last week though after sorting out all the coolant leaks though the thermostat to water pump clamp did open back up again and seeped so nipped that back up the other day. Anyway I found that with no more leaks the system would still hold a lot of pressure even over night/few days I initially put this down to the lpg leaking back into the coolant though was getting no bubbling or anything like that. Tried only on the petrol but actually was the same. Pressure isn’t building up so much that it’s shooting off hoses or loosing coolant even on long trips as I took it up to Yorkshire for the week about 100miles each way. Just not seeming to release so since I’d already ordered the cap and hose weeks thought you never know might sort it.
Sniff test is negative for exhaust gasses anyway
On the way up to Yorkshire with
@kermit_rr thermostat mod I could barely get it to temp. It just about sat at 12 maybe ever so slightly less on the gauge cruising along at 60mph the moment I went to 70 just to over take a lorry so for like 15 seconds the dial would go down from the increased airflow and take about 10 minutes to get to 12 again. That was on the Sunday before last in the day so it was decently warm
Coming back on Sunday just gone in the evening car was showing 13c the whole way back I couldn’t get it much past the first white line and round town it never really gets close to getting up to temp so I figure it worth swapping back to standard to see what happens
Thermostat hasn’t come yet though hopefully not waiting ages for it though as at this point I could have got it from one of the local motor factors quicker even though they have to order it in. and for not much more.
Oh and after cleaning up the underside of the engine before I went initially when I got to Yorkshire didn’t see any oil but when I got back the sump had a decent coating again. It’s actually starting to look like it’s the sump gasket rather than the front cover.
When I get under to the the thermostat I might see if any of the sump bolts need nipping up while I’m there.
I did do the Yorkshire drive all on lpg though and she did well with no issues even with those two slight leaks. Though did forget the gas filling cap at Morrisons in Wakefield… ordered another and put on today.