Not exactly "hat have I done on the freelander today, more what I've done at the the workshop today to make it easier to do stuff to the freelander tomorrow...
I got my two poster from a garage that was closing down, but it's a 3.5tonner, and with it being an asymetrical arm type of ramp, and geared for vans and minibusses, it ended up coming with ridiculously long arms on it, meaning on short wheelbase vehicles it was aye a challenge to get the vehicle in a sweetspot where the pads could land on the vehicles jacking points. And with the ongoing investigations into the freelander's lack of boost being an ongoing saga with lots of up, down, into the workshop, out for a test drive, back on to the ramp, this was really starting to grate on my nerves. And today when I went to put it on the ramp to pressure test the hard boost pipe that runs around the back of the engine, and had "missed" the position for the pads, the temper flared up, the landy got kicked out, and the heavy tools were brought to bare:
First move. sliced off the locking tabs to allow me to separate the inner and outer arm:
Next step, cut the back five inches off the inner arm:
Which as you can see here allowed it to go further back in to the outer arm:
The inner arm was then cut square at a reduced length (28.5") and hole drilled and tapped to screw in a locking bolt to prevent over extension fo the arm:
I then cut off the shims from the inner arms, and the offcuts there off, and replaced the short shim in the first pic on the inner arm with the longer shim from the offcut to increase contact area, although I put the phone away at this point for its own safety. Afterwards the shortened inner arm with the longer shim pad was inserted to the shortened outer arm, and captured by the lock bolt which catches the forward edge of that shim before the arm is overextended.
Following a massive tidy up, putting away the grinders + chop saw + welder + tapes + scribes + squares + PPE + extensions + discs etc... I then function tested it by bringing the freelander back in, and attempting to lift it. It was an order of magnitude easier to get the pads on the cars jacking points, so the ramp is definitely vastly improved by this modification, and the vehicle is now lifted:
There is a story to the BFG AT's on the hippo just now, "Missus Jay" kerbed the heck out of them when they were on her disco, fracking thing looked like a fifties caddy on sidewalls, my hippo usually runs kumho KL71's, but I acquired another set of hippo 16" rims, so replaced her AT's, put her old AT's on my hippo's new "summer wheels", which is what you see there. I've already put the socket on the rack-rack gun, and I've got the KL71's downstairs ready to fit, I might to that tomorrow, might wait till I get to the bottom of this turbo issue.
And you'll see hoses and gauges and stuff lined up ready for pressure testing tomorrow...
So tomorrow is when I'll do stuff to the freelander, but today's activities certainly made it easier to do these things. Given the amount of test drives that have been done, and the kerfuffle it was to get dead on that sweetspot for the ramp, if I'd done this modification before starting working on the hippo, I'd have had the damned thing fixed by now.