Yeah, i'm still here Tom
Wish I had more time to crack on properly, but it's all delay, Work, delay, Work, Work, delay and more bloody work ATM >:/
I promised an update, so here it is
I've been quiet, but not completely idle. Managed to get the Head back on the lump - we found the gasket was incorrectly fitted, AND the bolts weren't properly tightened, and the valves had been lapped previously with what looked like a drill and some road grit
Whipping the gasket off showed no3 wasn't sealing properly, and blowing into no4, plus the valves weren't properly seating.
1 gasket, 4 Valves and 5 hours of cleaning and hand lapping later the head was back on and ready to test for smoke.......it was a LOT better, but still not great.
Tied it down to the distro pump in the end, so shoved it on the clean bench for a partial strip - turns out the Auto advance unit had ceased up, so a quick clean and it again improved output greatly.
Still not right, slight intermittent misfire which moves around, and it's still dumping a bit too much, so i've sourced another one ( Thanks Sam! ), rather than shoving it on the testrig and faffing around for hours.
I've decided to replace the exhaust, seeing as this problem has been ongoing befoe I even got my hands on it - the box and pipework is probably saturated with diesel and oil.
Apparently, Bonnet hinges and hoseclamps can double up as intermediate exhaust mounts...
Nice clen underside, 70% done...
Prizes for my new game, "Where's the landy"
Got some painting done, and started on the doors and new hinges, too... Annoyingly, most of the Galvanizing is borked, so i'll have to paint all the cappings until such time that I can afford to get it all re-done.