Straight 6 rebuild

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Cheers guys, it could have really spoiled the weekend! Once bitten twice shy, I won't be relying on just the standard bonnet latch any more, I was trying to keep this vehicle as standard as possible but safety trumps originality in my books. With the vehicle being pained NATO green anyway some black rubber clasps a la military vehicles shouldn't look too out of place.

The matt NATO green paint that I have marks really easily (not that I'm overly fussed about that) so the sides now have some 'go faster stripes' from running alongside branches in the woods. When it's picked up a few more I'll go over them with a paintbrush.
 
Just read that from start to this bit (!).

I really enjoyed doing so, just wanted to say , thanks for sharing !!

ATB.
 
Drove to the MOT station this morning and was going fine till I indicated to turn into the garage at which point the indicator relay started clicking double quick, bugger, blown bulb or dodgy connection thinks I. Did a quick but of poking around in the car park but couldn't solve it so went and spoke to the garage to see if I could get 10 more minutes before he tested it to fix it, he said sure drive it in and onto the ramp and take as long as you need. He then lent me a multimeter and made us a cuppa while I fault found, turned out the earth wire had corroded where it joins the bulb holder so I was then given a reel of wire, crimpers and bullet connectors to fix it. When all sorted it was MOT'ed and came up with two advisories, first was a minor blow between the back box and the rear pipe of the exhaust so I need to give it another smear with exhaust paste, and the second is that on full lock the steering arm just touches the diff guard so that needs tickling with a grinder to give the arm full clearance. Nothing too major. When I went to pay there was no extra charge for the loan of the tools, ramp or delay in getting the test started, when I asked if I could pay for this I was told 'absolutely not'. :)
 
Aye, she's doing well, can't complain at all! The gearbox rebuild is now on hold as the missus wanted a log burner put in the house so there goes my gearbox fund! Got myself a ratty old canvas and sharks tooth rail on it at the minute, the truck cab and nice 3/4 tilt will go back on when the weather properly turns. Went out in it over the weekend to help deliver my mates 57 year old Fordson Major tractor from the Workshop where it's been for the last couple of months, through the centre of Bristol, along the A4, through the centre of Bath and out the other side to its new home. 5 of us took it in turns driving and having to stop every 20 minutes because the radiator weeps coolant when up to working temperature (we only found that out on the day!). Apologies to anyone who was stuck rolling along at 16 mph behind us! :D











PS - I discovered that 50mph with the screen folded down makes your eyes water lots...
 
A man after my own heart...love the old tractor...my mate has a nice old grey Fergie...he is like me...a life long Landrover owner.

Yes nice as it is...its not very practical driving with the screen down.

I re-built my gear box a few months ago...luckily I had an old box that I was given many years ago....it proved a very good source for donor parts as it had been re-built with many new gen parts...not easy to find now....so it did not cost me to much to do the job.

Nick.
 
Looks like I spoke too soon, I noticed a whiff of petrol round the back end the other day, looked underneath and the paint on the fuel tank has started bubbling along one seam. Bother. It's only a tiny amount of fuel that's seeping out so I've ordered some fuel tank repair putty for a fiver, hopefully that'll do the job otherwise it'll be £130 for a new tank plus a bit more for a new sender as the old one is pretty firmly in there.
 
Have been having fun and games with the gearbox for the last 2 weeks, a gearbox change has been on the cards for a while as the synchromesh on 3rd and 4th has been pretty non existent for the last couple of years, I've just been double declutching and it's not been too much of a problem. The plan was to get another box as a temporary replacement and refurb the original box at my leisure over the winter before switching the boxes again, I bought a 4 pot gearbox locally and managed to get hold of a 6 pot bellhousing for £25 so I got the two bellhousings swopped over and pulling the old box out.








After following the green bible's instructions of just undoing the rear propshaft from the transfer box and finding that there's not enough room to clear the bellhousing studs before you hit the prop I eventually removed the prop completely and the box flew out with no problems.



At least the box going in is a bit cleaner!

With the replacement box in place I did an oil change on it now that I could get an oil pan under it, the oil change came with a prize:



Bugger.

I filled the box up anyway and as the floor was still out and the propshafts still removed I fired up the engine to run it through the gears, all of the forward gears sounded fine but reverse was very different, quite clunky, not a good noise. I thought as it was a temporary replacement I could live with that so I got everything reassembled and took it out for a mile long test drive, when driving there was a clunking from every gear and a vibration from the gear lever. 'Bother' thinks I. At this point the plan changed, the new plan was to do a very quick refurb on my original gearbox, sort the synchro and as many bearings that I could get to with out splitting the gearbox from the transfer box and then get it back in the vehicle asap. I spent some time scraping all kinds of filth off of my original box and cleaning with gunk before opening the box, at this point it was fairly evident why the synchromesh didn't work, the last two oil changes I've found a synchrohub spring in the catch pan and had hoped that there'd be one remaining, apparently not, all were AWOL.


EDIT - photobucket apparently doesn't like this video, it just shows the baulk rings completely loose.

Started pulling things out:





The baulk ring looks ok but the dog teeth are knackered - junk.

This snap ring became the bane of my life for a while, 90 minutes later I was the victor.



Third gear used to whine, apart from the pitting there's no obvious wear but this is being replaced anyway.



The dog teeth on second were knackered too so that's going in the bin along with it's baulk ring that had similar wear.

My reverse selector fork had some 'interesting' wear on it, where the rest of it went (and when!) I have no idea, probably ground into a million tiny swarf particles over the years. New vs old, spot the difference.



This is everything that got replaced, primary pinion bearing, layshaft front and rear bearings, mainshaft front bearing, 2nd and 3rd gears from the main shaft, 3rd/4th synchro hub, reverse selector.



Then it was back to stripping the vehicle out again and swopping the box for the second time in 10 days, this time round it only took me 9 1/2 hours from picking up tools and getting things out of the vehicle to starting it up and taking it out for a test drive, for an 'enthusiastic amateur' working on my driveway I'm happy with that.





I drove the refurbed box a few miles and it's behaving itself, its really weird having synchromesh again, I'm finding myself still double declutching which I guess isn't a bad thing.

The ball bearing that came out of the replacement box was one of the detent balls, which one I don't know and quite why it's making noise I'm not certain of, it's possible the gears aren't meshed properly after having the layshaft disturbed when I took the bellhousing off, I'm not sure, I'll open it up at some point and have a look.
 
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It may be from 1st/2nd, I'll report back.

My box had no issues with popping out of gear or anything, there was a bit of a whine from 3rd and you had to double declutch to drive it without it crunching but the gears selected fine (even reverse with that dodgy selector fork!) and it drove fine, must have lots of built in redundancy in it!
 
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