Hello,
I need some help please....
1986 Land Rover 90 with a 200Tdi.
Noticed a lack of "power" last summer whilst pulling a twin jetski trailer out of the water on a steepish slipway - engine revs went up but no power.
It's not a slipping clutch and since last summer I've:
- replaced lift pump
- cut off the mesh filter on the bottom of the pipe in the tank
- bled the fuel filter
- replaced with new Silicone Turbo hoses
- repaced timing belt - and checked timing (all OK before and after)
- verified that the wastegate was not stuck
I assumed the problem had gone away as she drives OK but have not really put her under load (too cold to JetSki) but today I fitted a Turbo Gauge and am only getting a max of 0.3 bar of boost (both statis and in motion).
I shortened the wastegate bar by 3 turns and still max 0.3 bar - then I lengthened the bar by 2 turns (past it's original position) and still max 0.3 bar - have now put the bar back to where it was. The Turbo is spinning up can hear it and see it with the air filter hose off. There's minimal play in it as well.
I'm getting no smoke (black, blue or other) from the rear.
I've read that I'm supposed to be getting closer to 0.8 bar as standard which is quite a bit different from the measley 0.3 at the moment and would explain the lack of power noticed last summer.
I'm thinking stuck rod in the fuel injector pump but am very open to any other ideas??????
Help please
I need some help please....
1986 Land Rover 90 with a 200Tdi.
Noticed a lack of "power" last summer whilst pulling a twin jetski trailer out of the water on a steepish slipway - engine revs went up but no power.
It's not a slipping clutch and since last summer I've:
- replaced lift pump
- cut off the mesh filter on the bottom of the pipe in the tank
- bled the fuel filter
- replaced with new Silicone Turbo hoses
- repaced timing belt - and checked timing (all OK before and after)
- verified that the wastegate was not stuck
I assumed the problem had gone away as she drives OK but have not really put her under load (too cold to JetSki) but today I fitted a Turbo Gauge and am only getting a max of 0.3 bar of boost (both statis and in motion).
I shortened the wastegate bar by 3 turns and still max 0.3 bar - then I lengthened the bar by 2 turns (past it's original position) and still max 0.3 bar - have now put the bar back to where it was. The Turbo is spinning up can hear it and see it with the air filter hose off. There's minimal play in it as well.
I'm getting no smoke (black, blue or other) from the rear.
I've read that I'm supposed to be getting closer to 0.8 bar as standard which is quite a bit different from the measley 0.3 at the moment and would explain the lack of power noticed last summer.
I'm thinking stuck rod in the fuel injector pump but am very open to any other ideas??????
Help please