So i had a valve block at home i bought years ago for one of my old ones, i threw that on late last night, put it in extended height and used workshop compressor to fill it with air, lifted it right up pulled the battery off and was still up now over 12hours later,

Thrown it back outside and asked it to drop to normal height, front right corners still higher then the rest, so guess its out of calibration,

Did the fuel return lines looks like the intank pumps not working at all no flow through the filter with the glowplug light on,

It must have a later engine compared too my old ones plastic inlet and a maf and and egr (eeew)

Mabye a bit backwards in my process but iv not spent any thing before my holiday and its just been idle time iv been fiddling,

Im actually starting to like the brown interior too,

I now have a list to do before getting it in for an mot,

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Hmmm. Brown.
 
Back to doing l322 stuff 😅
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Drove from my place in Somerset to Cardiff.. or at least I would have if an EAS fault hadn’t shown itself just outside of Newport.

Managed to get off the M4 into a residential street with some free parking while it sat on its bumpstops. Bugger.

No worries, I’ve got the OBD cable in the glove box and my laptops in the boot. Have this checked and cleared and at least able to get to my destination and have a proper sort tomorrow.

All plugged in, run it and nothing. No codes present. Software is doing something as I can pull all the ride heights it’s at and get it to throw up the messages on the dash when selected. But the Unlock and Read Codes just isn’t doing anything.

So currently the P38 is in a street in Newport, while I’m in Cardiff to complete a training course this coming week. RAC will be called to recover me on Friday 🤦
 
Drove from my place in Somerset to Cardiff.. or at least I would have if an EAS fault hadn’t shown itself just outside of Newport.

Managed to get off the M4 into a residential street with some free parking while it sat on its bumpstops. Bugger.

No worries, I’ve got the OBD cable in the glove box and my laptops in the boot. Have this checked and cleared and at least able to get to my destination and have a proper sort tomorrow.

All plugged in, run it and nothing. No codes present. Software is doing something as I can pull all the ride heights it’s at and get it to throw up the messages on the dash when selected. But the Unlock and Read Codes just isn’t doing anything.

So currently the P38 is in a street in Newport, while I’m in Cardiff to complete a training course this coming week. RAC will be called to recover me on Friday 🤦
That is why I always carry a 12 volt tyre inflator and a set of emergency valves. Never had to use them but they are there should the need arise. Sounds like you pump has been feeding a leak and died as a result.
 
That is why I always carry a 12 volt tyre inflator and a set of emergency valves. Never had to use them but they are there should the need arise. Sounds like you pump has been feeding a leak and died as a result.
That’s my worry. I’ll no doubt post an update once I’ve dug deep. Doing various reading online it does seem like it’s a likely cause.
 
Had to dig out my a-frame & rescue daughter's Corsa. Looked like HG failure, but when I eventually got it apart the gasket looked ok, although the head does appear to have about 10thou warp. But my steel rule is not a proper engineers rule. Dropped the head off at Classic & Moder Enginbes in Bracknell for a skim.
 
What a pain in the bumtious. Smelt a faint diesel smell past couple of days so thought I'd have a look this morning. Leak off pipe no 5 to no 6 weeping at no 6. 2 minute job me thinks to change. Would it eckers like go on the no 6 nipple. Tried pipe off between 3 and 4, no joy at all. New piping fits all other injectors. Ended taking inlet manifold off for a good look see. Got big torch out and magnifying glass. Well blow me a ring of the old leak off pipe had stayed on the nipple. Cut off carefully with Stanley knife and voila on went the new pipe. So what started out as a nowt job turned into a saga, at least a happy ending :D
 
What a pain in the bumtious. Smelt a faint diesel smell past couple of days so thought I'd have a look this morning. Leak off pipe no 5 to no 6 weeping at no 6. 2 minute job me thinks to change. Would it eckers like go on the no 6 nipple. Tried pipe off between 3 and 4, no joy at all. New piping fits all other injectors. Ended taking inlet manifold off for a good look see. Got big torch out and magnifying glass. Well blow me a ring of the old leak off pipe had stayed on the nipple. Cut off carefully with Stanley knife and voila on went the new pipe. So what started out as a nowt job turned into a saga, at least a happy ending :D
It's a land-rover thing🤪
 

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