Hi mate, the saga continues. One thing I have noticed is when I remove and replace things the suspension behaves differently. Yesterday the exhaust valve was running pretty consistently with only a couple of minutes in-between. Today not so much.
I got the suspension up to standard and did a guided recalibration. After this, I pulled fuse 26 and interestingly the rear lowered slightly and the front went up both by 1" respectively.
I will post up a couple of screenshots, but no issues with the pressure relief valve or the ride height sensors from what I can see.
I checked a lot of the wiring connections as per the diagrams. I was unable to locate the blue or grey plug, there is one nr the LH headlight that is connected into the suspension harness. it only has red and green/yellow. It is not as pictured and is a black plug.
I had a look at the wiring plug above the rear LH wheel. Not tested for continuity yet, but nothing obvious.
I unplugged the ECM and checked again. Nothing obvious. I still need to do a continuity test.
Added a wire to the blue/black wire at the ECM and connected it instead. It behaved the same but recorded at 5v instead of just under 4v as I have been seeing consistently. Not sure if that is meaningful. If the ECM is not able to provide a strong negative trigger this may result in what I am seeing with the extended negative trigger until the pressure builds up to release from the exhaust valve.
I removed and replaced all of the ground wires on the A-pillar drivers side. No obvious issues.
Right now it is at offroad height, but thinks it is standard. I have pulled fuse 26 to see what happens overnight.
I should have an hour or two Monday evening. If it has not gone down overnight I may use it as is to buy some time to figure out next steps.
I am curious if this is a new fault or something that was masked by the previous pump leaking from the drier end cap. Otherwise, it seems strange that it coincided with fitting the new pump.
Last thing I tried this evening was to swap out the relay and fusible link with the LR4. I had already swapped the relay with the engine management relay, but thought it was worth doing.
hi mate
good to see u at least have a heater, also as a side note I’ve seen cold can cause issues
does seem strange on what the system is doing , because when I bought mine it was in a terrible mess, needed a total wire trace , replacing compressor, air tank, 3 x valve blocks , then sorting out the bodges , insulation tape etc
I started battery disconnected , finding all the connections and pulling them off everything , done continuity on each one and fixed accordingly , then as I reconnected a pair of connection used a multimeter to ensure continuity was ok on both sides, proving the pins were sound
Apologises I’m gassing again and side tracking , trouble is with the D3 there’s so many connections, / ground points hidden away , just need 1 or 2 to relay start causing spurious errors
feel the connector that at the air compressor that carries the pressure sensor and exhaust extremely important , alas the pressure sensor is ok by ur readings
sounds like u may have to start doing voltage drop tests
Bless u for the updates and can see behind the scenes so to speak youve spends endless amount of hours
there is also an extensive amount of info in the D3 forum, mainly because of those connectors which may be in a different position on the LHD LR3 , which of course the main goal is to get to the bottom of the issue
shame ur so far away as I’ve on many occasions gone out or they’ve come to me and helped where I could , never had a system beat me yet and can see ur the same
https://www.disco3.co.uk/forum/
never know someone on the D3 forum may be near u, or someone has seen the same fault
will keep searching and course help all I can from this end
keep warm mate and will be interesting to see what the outcome is from the removal of the F26
like wise , have a good one mate and will of course post if I find anything new that may help