Update...
Cleaned connections to fuel cut off switch, and cleaned the fire trap breather and hoses. Also cleaned and inspected connection to charcoal filter.
As matter of course I removed the stepper motor (it’s only a week or so old) and cleaned. I did notice when removing it that it wasn’t as tight as it should have been, assuming it’s worked loose with expansion and contraction from temps. I also spotted a vacuum hose below the stepper motor, the end nearest the throttle body was badly perished, I’ve replaced with new and refitted the stepper motor.
Still a cold engine, I fired it up, it idled slightly low (just below 750rpm) until I have a slight blip of the throttle (blip no more than 1200 rpm) and it then settled quickly to 800 rpm.
I shall pop out later on today and see how this goes, I’ll update later.
Thanks to all so far, I know these issues are common, your probably sick to death of hearing the same questions!
Cleaned connections to fuel cut off switch, and cleaned the fire trap breather and hoses. Also cleaned and inspected connection to charcoal filter.
As matter of course I removed the stepper motor (it’s only a week or so old) and cleaned. I did notice when removing it that it wasn’t as tight as it should have been, assuming it’s worked loose with expansion and contraction from temps. I also spotted a vacuum hose below the stepper motor, the end nearest the throttle body was badly perished, I’ve replaced with new and refitted the stepper motor.
Still a cold engine, I fired it up, it idled slightly low (just below 750rpm) until I have a slight blip of the throttle (blip no more than 1200 rpm) and it then settled quickly to 800 rpm.
I shall pop out later on today and see how this goes, I’ll update later.
Thanks to all so far, I know these issues are common, your probably sick to death of hearing the same questions!