TwoHundredTeeDeeEue
New Member
Morning all.
Replaced HG on my 200 TDI recently and put a 2nd hand head on (looks in decent nick, cleaned up valves and fitted new stem seals). I did balls it up and put gasket top-down initially (it was dark, that's my excuse..). Tried starting, sounded like low/no compression as turn over was really fast. Realised oil leak from front of cylinder 1 and the thickness marker on gasket was behind diesel pump so knew what I'd done. Took it all off again, refitted with new HG. I still have the same starting issue but no leaks this time. There was some coolant in the cylinders after my previous mistake.
Compression tests on all cylinders showing only 3-5 bar. Leak down results were pretty good, took rocker shaft off to ensure valves were sealing and they seem to be acceptable.
Any suggestions on what I might have done or what I do next? Main concern is I've bent the con rods and not getting compression due to reduced piston travel so I'll need to take the head back off to check that anyway. Seems a bit extreme that would have happened just turning it over from the starter for a minute or two though.
Replaced HG on my 200 TDI recently and put a 2nd hand head on (looks in decent nick, cleaned up valves and fitted new stem seals). I did balls it up and put gasket top-down initially (it was dark, that's my excuse..). Tried starting, sounded like low/no compression as turn over was really fast. Realised oil leak from front of cylinder 1 and the thickness marker on gasket was behind diesel pump so knew what I'd done. Took it all off again, refitted with new HG. I still have the same starting issue but no leaks this time. There was some coolant in the cylinders after my previous mistake.
Compression tests on all cylinders showing only 3-5 bar. Leak down results were pretty good, took rocker shaft off to ensure valves were sealing and they seem to be acceptable.
Any suggestions on what I might have done or what I do next? Main concern is I've bent the con rods and not getting compression due to reduced piston travel so I'll need to take the head back off to check that anyway. Seems a bit extreme that would have happened just turning it over from the starter for a minute or two though.