Defenderer
Member
Hi Guys and Gals
My 300tdi defender went gutless on me.... Seemed decent through the low gears and flat cruising but show it even a mild hill and it's down through the gears.... Pulled things down and lots of oil in the intake side (turbo seals failed).... Bought a boost gauge and only about 4psi maxed..... Went through the lot, pipework, intercooler, air filter, no leaks or obstructions (and no black smoke).... Moved on to fueling, changed filter, checked lift pump pushing fuel out of bleed on filter nicely, opened the top of the pump and the fueling pin seems to pop out nicely, diaphragm sound and blew down the actuating pipe from the turbo end and no sign of leakage.... Exhaust seems to be blowing through nicely and not obstructed.... Changed turbo and just the same.... No boost and couldn't pull its trousers up!!..... Went through the lot again (most of it more than once).... Running through my store of head-scratching and thought I'd try here before admitting miserable defeat and taking it to a garage (never like doing that!!)
Any thoughts or things I've missed...... Have thought that my Web purchased boost gauge may be duff, but the lack of pull is real enough.... Also the lack of black smoke is odd for a poor intake pressure (however caused).... Don't know enough about turbos to know if poor fueling/power would perhaps lead to low exhaust flow and therefore low boost..... Starts and runs under light load just fine.
Any thoughts gratefully received
Cheers
Keith
My 300tdi defender went gutless on me.... Seemed decent through the low gears and flat cruising but show it even a mild hill and it's down through the gears.... Pulled things down and lots of oil in the intake side (turbo seals failed).... Bought a boost gauge and only about 4psi maxed..... Went through the lot, pipework, intercooler, air filter, no leaks or obstructions (and no black smoke).... Moved on to fueling, changed filter, checked lift pump pushing fuel out of bleed on filter nicely, opened the top of the pump and the fueling pin seems to pop out nicely, diaphragm sound and blew down the actuating pipe from the turbo end and no sign of leakage.... Exhaust seems to be blowing through nicely and not obstructed.... Changed turbo and just the same.... No boost and couldn't pull its trousers up!!..... Went through the lot again (most of it more than once).... Running through my store of head-scratching and thought I'd try here before admitting miserable defeat and taking it to a garage (never like doing that!!)
Any thoughts or things I've missed...... Have thought that my Web purchased boost gauge may be duff, but the lack of pull is real enough.... Also the lack of black smoke is odd for a poor intake pressure (however caused).... Don't know enough about turbos to know if poor fueling/power would perhaps lead to low exhaust flow and therefore low boost..... Starts and runs under light load just fine.
Any thoughts gratefully received
Cheers
Keith